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Weird Rev limit.

Posted: Sun Aug 17, 2008 10:01 pm
by FrodoGT
Ive noticed recently a strange occurrence with my s300 unit, which is installed in a p28 ecu.

Sometimes randomly (at least it seems random) while trying to pull away from a light (or rev the car at all) the rev limiter kicks on at a measly 3500 rpm. It does this usually in each gear and it sometimes stops mid gear and lets me past 3500. Usually 3rd. But tonight I noticed that if I shut the car off while driving and then proceed. It runs fine. But if I stop the car, say at a light or something..I then cant pull away from the light, again. This is starting to aggrevate me. At first I thought it could be the vss signal and the car was stuck in launch control..but my launch control is set to 5k so its most certainly not that, also I finally managed to catch it on a datalog and watched what happened. Rev limit right on at 3500, no CEL's No warnings. Nothing.

I do notice thought that when it does this just before it hits the limiter there is a huge loss in power as if the timing is being drastically retarded, or there is a ton of fuel being dumped. While its running in this mode the exhaust will pop and crackle while in decel and the idle is a little rough and the car will die in a short time if I don't move.

Any time this isn't going on the car runs perfectly though. It seems as though something is kicking the ecu into a safety mode.

Any thoughts? Ive already checked every wire I could on my jumper harness, my gauge cluster, and under the hood. None of my solder connection are loose or change the way the car runs at all.

Posted: Mon Aug 18, 2008 7:18 am
by Hondata
You're probably getting an intermittant fault on a sensor or sensor wire. You will need to datalog until you catch the error occuring.

Posted: Mon Aug 18, 2008 12:17 pm
by FrodoGT
I think it may be an injector wire. I played with my connections on my mpfi swap just off the jumper harness and the car started to run rough..almost like a subaru. when I tried getting to 3500 it broke up just before and threw an injector code and wouldn't pass 3500. Unfortunately I didnt get to test this because I broke the jumper harness but I will check it out once its fixed later tonight.